Hardware Development - Motor
Since the motor simulation is working, I decided to test the program with the hardware. I used Galep-5 Universal programmer to program the PIC. The code was successfully burnt into the PIC. Then, I used the SK40C PIC development board from Cytron to interface the PIC with the motor driver. Unfortunately, the motor still did not work. I tried a few times but still there is no sign of motor movement, back to square one. I added an array of LEDs to check whether the motor sequence is running but the LEDs also did not working. Again, I checked the connection, the power supply and measure the input and output, but still did not give any clues what is going on. Why it fails to operate? I’m really, really tired and I decided to continue tomorrow.
Galep-5 Universal Programmer |
SK40C PIC Development Board |
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